Core 1 wouldn't read the pull switch on MP5. Found a loose connection in the core plug.
When DR18 was started it would index then trip the main breaker to MP25. The process heaters were shorted. I replaced them and started it back up.
The robot on MP25 crashed in the core dummy plug. Straighten the robot arm and set it to rotate above the belt instead of the mold.
Collin Miller
No comments:
Post a Comment