There wasn't enough operators to run the hoky top covers tonight but Charlie and I went ahead and syncronized the robot on 22 with the ejectors. With the robot running at 100% global speed, the ejectors need to be set at 28%. We moved the cups and also dropped the EOAT positive stop bar down to keep from hitting the runner.
Also while setting up number #5 robot the CPU faulted out and had to be cleared. I noticed the pentant light is almost out. I'm not sure if we have any hid away anywhere. If not it I can order some and make them a stocked item.
Collin
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