Got MP2 running today, but the eject option I tried to add never did work. The software did not want to cooperate. How it is running now is that I have the ball valves cracked a little and I’m just reading the butterfly position, not the switches on the mold. I also turned on the core 2 option, but I never tried it out. They needed parts and we’ll just deal with it later.
Robot on MP7 is ready. X axis was not reading position.
MP10 bowl feeder still needs a little work.
Thanks
Joshua Ledbetter
Manufacturing Engineer
Oreck Manufacturing Company
931-239-3235
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