Finished repairing the connector nest for vibratory welder. Replaced broken/missing screws loctited them. Cleaned and inspected the tool. It looks like the adjustment method they have been using requires a hammer sometimes.
Lubed all of the tiebars and refilled reservoirs and greased the machines.
We need to get a repair kit for the Milacron machines complete with 3/16" nylon tubing and the ferule type fitting they use.
MP#15- has a broken lube line that needs repaired when it is down.
MP#17- has an extruder hose that is leaking. I tagged and measured it. Made a new hose up and left a note so we can change it when it is between molds.
I left a note on the Fastenal board to restock the "assorted springs" drawer. I used a spring last night to repair one of the gasket locating tools (used on the intake pivots) but didn't really have what was needed.
I left the old clamp tonnage transducer with Mark so we can possibly stock a spare.
Replaced the cabinet fan on robot #3 panel.
Basically fixed little things most of the night and helped the techs because this shift has no tooling person. We repaired the tool on press#22 that broke out all 4 keen-serts. There were only 2 left in the box so we patched it up to get it running.
Let me know how you want to do that blocked nozzle test. I am supposing you want to do a dynamic check ring reliability test for bad screw tips?
I plan to take off this evening but will work on till Friday night. Call tomorrow if there are any questions.
Sean
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