Thursday, December 30, 2010

12.29.10 - D shift - Sean

Worked with Mike Daniels on PM's all night.

Nothing Major happening worth mentioning.

Hope next year goes as smoothly as tonight did!

Call if you need bailed out of jail! Happy new year team!

Sean

Tuesday, December 28, 2010

12.27.10 - D shift Sean

Mp#5- Cores not working...found loose terminal strip on Output card 6

MP#21- Bleedoff at Nozzle. Took out 3 heaterbands and thermocouple. Looked like the sled forward switch had worked loose causing the problem. Had no more trouble after we started it back up.

Mp #2- Zone 3 had a bad band. Replaced it. Replaced the fuses and checked operation...O.K. to run.

Continued with PM's. Worked on #10 press and robot tonight.

Call if you have any questions. Have a successful day!

Sean

Monday, December 20, 2010

12.19.10 D shift Sean

Mp#8- Replaced the ejector hydraulic hoses. They had been red tagged since 2008, so i replaced them and checked operation.

Continued working on PM's.

Need to order some cabinet fans again in 120VAC.

Have a great day!

Sean

Sunday, December 19, 2010

12.18.10 D shift - Sean

Continued with PM's...Presses and robots #2 and #4 tonight.

Had an issue with #23 ejector encoder was not reading right after they set a mold in it.

I changed the offset on the VRE encoder offset and it started working correctly. I did check to see if anything was loose on the encoder first but it appeared tight.

Sean

Thursday, December 9, 2010

Ronnie Upchurch

                   12/08/10

 

Worked on fascia hot stamp.

 

MP-13  Pulled barrel cover & cleaned off blow back – ¾ down the barrel. I was able to save heater band wiring & the covers , with some minor body work.

 

MP-19 The DME t.c. was reading low , but the mold heater was running away. I found that the t,c, wire had been pinched behind the mold clamp. Replaced.

 

 

                   12/09/10

 

MP-13  Pulled  the Conair heater to get the part #. There were two possible numbers for that model.  I ordered replacements .  There are only two heaters

       Per zone – 240 v.

 

MP-10   We cleaned out the nut feeder , Again , & cleaned a box of nuts. Mark adjusted the tracks.

 

MP-26  The center knock-out mounting stud on the eject. plate fell off.  Reinstalled.

 

I ordered a new adjustment screw & nut for MP-24 spacer adjustment.

 

I sent the top cover drill out for repair.

 

I ordered a new replacement motor for the small Solo grinder.

Wednesday, December 8, 2010

MP05 Robot

MP05 Robot has been stopping the last week or so randomly with a “Mold is not open- Robot in Unsafe Position error”. 

ANYTIME you get this error it means that the mold is not at it’s Open Limit and also the robot is not on either the Y-Up safety switch or Z-Out Safety Switch.

The Power Supply was low and what was happening was the 20 VDC that made it back to the coil on RYS or RZS would allow it to drop out one or both of them every now and again.

 

Mark adjusted the PS up to around 26VDC and fixed the problem.

 

Thanks

 

Joshua Ledbetter

Molding Maintenance Manager &

Manufacturing Engineer

Oreck Manufacturing Company

(C) 931-239-3235

(F) 931-646-7615

 

Monday, December 6, 2010

12.5.10- Dshift Sean

Mp#24- Made a new "bushing replacement part". Checked operation, O.K. to run.

Worked on PM's.

Replaced damed plugs on #10 connector mold from where it had been damaged before.

Made some adjustments to the nut press so nuts would slide down correctly.

Started making another component for the fan mold in #25, to grip instead of using the vacuum cup. (Requested by Darryl B.)

Call if you have any questions.

If you are reading this it is because I did post a blog...reciprocate the info!

Knowledge is power! Share the wealth!

Thanks,

Sean

Sunday, December 5, 2010

Ronnie Upchurch

            12/03/10

 

MP-25   Replaced a broken air quick connect fitting on robot eoat.

 

MP-10   Added hydraulic fluid.

 

I helped Josh & Mark get old press 13 moved out.

 

I replaced the pneumatic drill on the top cover fixture. I will send the broken one out for repair.

 

            12/04/10

 

Moved the home sensor block over some for the single cavity connector mold.

 

Worked on the degate & lable fixture in shop.

 

MP-5   The tech said that core 2 on the top cover mold wasn’t pulling. I found the bottom core not hooked in to the cylinder.

 

            12/05/10

 

MP-22   PMed  the robot.

 

I  mounted  the motor on the polisher  test fixture table.  It’s the one they test the brush pans on.

 

Cleaned up some in shop.

Tuesday, November 30, 2010

11.29.10- D shift Sean

PM'd- MP#25 machine and robot.

Dryer DR#6 on mezzanine alarm for Regen Overload. reset OL's and had no further problems with it.

Hope everyone had a great Holiday. Call if there are any questions.

Sean

Friday, November 12, 2010

11.11.10 D-shift Sean

Mp#7- Robot PM. Had to use 2 of the spare air lines on the Y-axis arm, they were leaking. Inspected it thoroughly, cleaned and lubed. Ready to go.

Continued training on the robots with the techs on this shift.

I will continue touching up the presses with a little paint as they are down. I just need some roller pads and a roller handle if somebody happens to go to Lowes any this week or next.

Also, it should be noted that yesterday, before I left, Darryl had asked me to help him repair #24. Apparently they had tried to put two full width spacers on the clamp and it had worked loose and possibly damaged the threads? He got it started and reassembled, but thetre may still be some damage and further problems when the spacer needs to be changed out again. FYI.
The mold setter on D shift knows more about it.

Call if there are any questions.

Sean

Thursday, November 11, 2010

11.10.10 D-shift Sean

Made a drive roller shaft for the small conveyor. Installed it and reassembled the conveyor and checked operation. O.K. to run, located it in the auxilliary equipment area.

Also moved the Milacron dryer to auxilliary equipment area as well. It ran most of the night without incident.

Mp#23- Darryl said that Bill and his techs were able to run the 2-cavity fan with the conveyor turned out away from the press and unload the parts 4 across the belt.? He asked me to set it up to do that but I was not able to make the crosswise move during Pack 1 or Pack 2. When I changed the modes, it changed on both Packs. Any idea how they did this? I would like to know.

Continued working on Pm's.

Painted the angle iron brackets Yellow with spray paint. It is a light coat but all I could find.
There was some driveway marking paint that was very flat and I didn't think it was a good idea to use that.

What was the story with 17? I heard it went down for maintenance? That we are shopping for a replacement?

Call if there are any questions! Have a great day!

Sean

Tuesday, November 9, 2010

Ronnie Upchurch

   MP-5  Replaced the nozzle heater band & fuse. The wire broke off & shorted out.

 

  MP-17  Cleaned up – changed out pads- emptied jug.

 

  Sean fabricated a motor-mount belt tension bracket & a safety switch block. I tapped out the 10 mm holes & mounted the bracket & block. I also installed the blades.

          We still need the key for the safety switch & knobs for the block handles. I sent Mark the part numbers.

 

 

Wednesday, November 3, 2010

Ronnie Upchurch

                         11/01/10

 

MP-13  Blow back – tightened down sled & replaced 2 nozz. bands.

 

MP-15 Solid state relay on nozz. heaters was staying energized – rebooted press & is working fine.

 

MP-9  Need to look at building new eoat for handle mold. The small cups don’t hold good on textured parts.

 

Brought grinder in from trailer. The repair parts came in.

 

                        11/02/10

 

MP-14  The timer relay on the thermolator went out. Replaced & Mark ordered more.

 

MP-11  Mold hanger broke a switch & a fitting on the core cylinder .  Mold # 75033.  Mark repaired.

 

MP-3  The Z axis contactor went out. Mark installed a new contactor & overload.

 

MP-21  A water pipe broke in the stripper plate – fan mold. Tooling  removed the broken threads.

 

MP-5  The wheel press staying down after pressing the wheels in.  Someone had turned the pressure up too high & the over stroke switch was making.

          Readjusted to 100 psi.

11.2.10 D shift Sean

Mp#2- had some problems with the core pull switch not reading. I went through it several times and it will read for awhile then quit again. We put it on timers til it comes out again.

MP#5- the base plate press needs a block to support the spring, and another spring detangler made up so they can run them both. Not urgent at this time.

MP#4- had to modify the gate cutter fixture to accomodate the change to the runner location on the tool. Works fine now.

MP#10- Nut Press. Cleaned out the vibratory bowl, tracks, and rails. Stoned the scratches out as good as I could. Noticed that the upper metal rails are magnetized and caused my screwdriver to become magnetized as well. I think an option to help prevent them from hanging up so bad would be to created new upper rails from a different material such as aluminum or plastic?

Helped the technicians and mold setter, set-up the mold and robot on #1,(at their request). They were not sure how to hook up the core hydraulic unit, etc. and we got the robot programmed in and going good. Also showed them how to save programs in all of the star robots again.

Mp#9- Robot is stopping intermittently above the conveyor, either going up or down. I slowed down the speeds and it seemed to reduce the frequency. I tried to watch it as much as I could but got called away. The vacuum switch is adjusted correctly so it is not that. I watched the brake modules and they were working correctly when it stopped once. I think it is probably a loose connection, but they did not want to shut it down completely for me to look at it.?

Went over the access receivers in the mezzanine. Several had loose screws and were loosing suction, etc. In general I looked around for anything else that might need repaired, etc.

Call if you have any questions.

Sean

Monday, November 1, 2010

Ronnie Upchurch

                 10/27/10

 

MP-12   Blow back -  the mold wasn’t centered in the check ring. I replaced one nozz. adapter  heater band.

 

MP-17 Cleaned up oil.

 

                10/28/10

 

MP-10  Cleaned oil from nut feeder. I gave them some alcohol & a bucket to clean nuts. Mark emailed engineering so they can contact vender.

 

D-32  Alarm  11  -   The turntable switch was out of adjustment.

 

MP-6   They changed to polycarb on the base plate. Mark turned the pressure up on the wheel press.

 

MP- 25 Set up chute for hokey handle water cooling tank.

 

Friday, October 29, 2010

10.28.10 D shift Sean

The robot on #6 has been dropping the parts into the grinder off/on all night. The cause is that the press will often mold baseplates with too much flash on the runner. This causes the gate cutters not to completely cut through the gate. This in turn causes the runner gripper to hold onto everything until it drops all of it into the grinder. FYI- ?

Replaced the regen heaters and the regen blower on DR#5. It is in the shop looped out until the cans have cycled enough to run on the floor.

Mostly had problems related to people not understanding how things operate correctly.

Did PM on 21, press and robot.

Also, the water bath operation for the Hokey handle was requiring them to hand dry each part with an air blow-off tool. I put up a cart with a wire frame basket and a fan blowing down on it so they could spread them out and most of the water could dry off before they got to the drying stage. We may want to look at that operation again for improvements?

I will probably come in sometime this weekend to discuss PM's with Mike. Likely on Sunday night early.

Call if you need something. have a good weekend.

Sean

Thursday, October 28, 2010

10.27.10 D shift Sean

The Square nut press on #10 has problems with sticking due to the unusually oily nuts. I cleaned the entire vibrator bowl out and wiped out the slide tracks, but, until the nuts are degreased better, they will continue to get stuck.

I asked Darryl to speak with Wayne McConnel about looking into this oil issue with the vendors possibly? I do not remember having this problem when this began, do you?

Darryl said they had always been that way and there was nothing he could do, it would cost Oreck more forthe supplier to degrease them.?

Anyway, there it is.

Mark and I arrived at a PM program draft proposal which should be implemented soon for our team.

Other than that I continued with PM's.

The Robot riser has been painted and should be dry.

Call if I can help in any way!

Sean

Saturday, October 23, 2010

Ronnie Upchurch

              10/22/10

 

MP-16   Installed a flow control valve on the eject. retract line.

 

MP-21  They changed the nozzle tip from a button tip to a  2”.  I installed a tip heater band and replaced the adapter band that was burned out.

 

MP-17 Cleaned up oil, emptied jug, & replaced pads…………………………..

 

MP-4  At 5pm the tech told me the robot crashed. I checked & the “Y” axis had extended to the mold & hit the stationary side. It broke the “C” air

          cylinder, two vacuum fittings, & bent two suction cup brackets. I removed the eoat & cylinder & turned it over to Sean Man.

 

              10/23/10

 

MP-9  The “Z” axis set point was drifting. I checked the encoder – everything was tight. I tightened the “Z” axis belt & rebooted the robot. It looks

          consistent now.

 

MP-22  The hotstamp heats kept going off. I checked all the heater connections. I reseated the T.C. plug on the board. It’s running & hasn’t cut off

            in four hours.

 

MP-11  The PS-2 pressure switch on the injection unit quit working. I replaced it.

10.22.10 D-shift Sean

Mp#4 Robot- repaired the C-axis wrist cylinder. The threads had snapped on the cylinder shaft when it crashed on Friday. Drilled out the end of the shaft and tapped it for set screw. Reassembled and tested operations. Replaced 2 broken fittings on the vacuum cups. It will run for now until we can get a replacement cylinder on order within the next few days.

Mp#9 Robot- The Y-axis was not homing in the same place and eventually would not home, although it was still referencing. Found the Y-home switch "flag" had loosened and slipped down. It took several attempts to locate it correectly until it would operate correctly. Also inspected the encoder, bolts, and belts while up there.


Had another water leak on MP#1- broke some of the same water lines on the fan mold (same reason as before on 21).

Luckily there was not any water spray to cause damage to the robot or injection molding machine.!

Call if there are any questions. I will not be in tonight for PTO time. Have a great day!

Sean

Friday, October 22, 2010

Week of October 18, 2010

Made program changes to the PLC and Quickpanel on MP5 Robot for an I/O Monitoring Screen.  The new screen can be accessed from the main menu.  Please try to check it out and use it as much as possible, we need to see if everything works correctly and if we want any more changes.  If you have any questions or suggestions please let me know. 

 

Picked up an inline, directional control valve for the eject retract on MP16 to slow down breakage of butterfly bolts.  Ronnie installed and set it to smooth out the banging on the retract.

 

We received the replacement seals for the Novatec Proportional Valves.  They are in MRO.

 

Small ice cube relays were ordered for the AEC Robot control cabinets, RB, RYS, and RZS.

 

The new butterfly plate, guide rod, and knockout rods for MP20 were finished and Gary installed.

 

Helped Mitch set the welder outputs in MP12.

 

Tightened and realigned clamp cylinder on MP10 connector welder.

 

Ordered the steel for Robot Riser spacers.  Josh got the prints for the machine mounts.  The steel should be here this Saturday.  We can start making them next week.

 

Started working on In Mold Labeling Project

 

Changed out more of the 3 pin color pumps connectors to 2 pin.

 

Mark McKee

Technical Specialist

Oreck Manufacturing Company

1400 Salem Rd

CookevilleTN  38506

mmckee@oreck.com

PH      931.646.7856

CELL  931.644.5289

FAX    931.646.7615

 

Wednesday, October 20, 2010

10-18-2010,

Good Morning Gents,

 

Lots of little stuff last night like plug it up turn it on.

Had issue with mp5 the cores not always working reseat I/O boards and they seemed to work for a sort while. Finally found a very loose wire on board in #6 slot in control rack.

 Hasn’t missed a lick since.       

 

Not really anything else major to speak of.

 

Have Great Day

Mike

10.19.10- D shift

Mp#9- Robot kept stopping, It was stopping over the conveyor every time. I noticed the speeds on the axis were all maxed out. I slowed them down to around 9800 each and it did not stop anymore afterwards.

Mp#10- Robot did not stop any at all tonight. Good Job guys!
Vacuumed oil out from under 10 also.

Mp#2- replaced nozzle heater band and fuse from bleedoff. Had to burn out the sprue plastic with oxy/acetylene torch.

Mp#16, Mp#19- PM'd.

Mp#8- Fan Housing press had problems with the nut press die magnet/ locating pin getting stuck inside the recess orifice. Took the one off the spare press and replaced it.

Left the damaged one in the shop for Gary or Mike to make a new one by...maybe?

Call if there are any questions.

Have a great day!

Sean

Friday, October 15, 2010

10.14.10 D shift-Sean

Mp#11- Sled would not go back. removed the V26 solenoid valve assy. and cleaned out the check valve and orifices with solvent and air nozzle. It appeared to be clogged and dirty. Reassembled, checked operation, O.K. to run.
Also refilled with about 20 gallons of Rando 46 hydraulic fluid.

Mp#23- Nozzle was not heating (according to the tech). Found band clamp broken and the other one missing. He still wanted to change the band out anyway, so we did.

The ink pad printer nest assy appears to be loose but all the screws are tight on it. Mostly looks like slop in the xy table, except too much ? I also could not locate the manuals for it. The last time I knew where they were was inside the pad printer. Now no idea? I was going to see what kind of pm inspection it needed?

Call if there are any questions, have a great weekend.

Sean

Thursday, October 14, 2010

10.14.10 D shift

Mp#15- Zone 1 overtemp.

Found the problem to be an incorrect thermocouple type. It had a "j" type and it should have been a "k" type.

There were 2 more J type in the MRO location where the K's were supposed to be and I almost made the same mistake that someone else had made, of putting one on. Instead I used a nozzle band K type and put it under the band on the first zone.

It is running good and staying exactly on temperature now.

Fixed the leak on MP#2.

Refilled 17 with oil and cleaned up the oil dry.

Checked out the milacron dryer DR17 and it is fine.

Checked out DR2, looped it out for a few hours and checked the beds, it is fine too.

Sent an email to one metal supplier to see if they can get us some brass peices for the sled shims the right dimensions that I measured tonight.

Be back at 2pm today.

Don't call, I won't answer....lol.

Sean

thermocouple calibrator

This is the lowest priced calibrator I found on the web at $195.00

http://www.omega.com/pptst/CL3512A.html

Omega's are a good brand and this tool will allow us to read the output from a thermocouple or send a signal to a temperature controller for comparison or tuning.

With as much machinery we use with temperature related controls, this tool is a must for any professional maintenance department such as Oreck's.

Check it out!

Monday, October 11, 2010

10.10.10 D shift weekend Sean

Mp#1- was making a squeaking sound when the screw was almost complete with building a shot. I greased the extruder bearing assembly but that did not appear to be the source of the sound. Then I actually put a little grease on the screw itself at the back of where it entered the barrel and it seamed to help. It did not run long enough to know for sure though and likely needs to be inspected further when it starts back up.





Mp#3- Had an E00240 error. Had to reboot from the boot card. Then we had to reload a set-up in it. Ran good the rest of the day.



Mp#5-had leaks from where someone just left a hose dragging beside the clamp.



Mp#2- Has a leak on the core/ejector hose valve block we installed for the steamer molds. When it goes down we can re-do it. Put it on a shared tasks outlook item.



DR#6- Finished what Ronnie was working on and replaced the desiccant in all of the canisters. Checked it out with the Dew point meter @-40. Tagged it and located it in the mezz room.



We have been seeing quite a few dryer issues lately. I followed the email suggestions for testing the touch pad on that Cincinnati dryer/hopper and it appeared that the display board is likely defective as jumpering the touch pad pins gave no response.



Checked out several DME cards, replaced fuses and tested them on a mold. They all worked fine. Tagged them and put them back out on the shelf.



Worked on PM's all weekend. Finding many issues with loose components on the loading system. Also finding robot Y-axis are getting loosened. Tightening them up, and other wrist components are getting loose.



One issue that we need to start getting into is the sled shims on these Nissei machines. Many are working out from under the sleds. I think we can get some brass the full length of the guides and secure it with screws? The problem is that we will have to schedule them down and figure out how to get them elevated enough to install them. Shouldn't be too much of a problem. I will measure all of them that need repaired now and come up with a parts list on Thursday morning.



Since Ronnie is going to be out on the

Sunday, October 10, 2010

Ronnie Upchurch

I emptied all the overflow jugs on the presses, cleaned up the oil on MP-17, & vacuumed the pan on MP-6.

 

MP-4   I made an eoat for the rear steemer handle mold & installed it.

           Somebody left the air poppet fittings out of the mold. We found them in tooling & installed them.

       

 

D-6  ran in the maint. shop for nearly 24 hrs. & the beds never did dry. I started pulling the desiccant cans to change them out.

Saturday, October 9, 2010

Ronnie Upchurch

 10/8/10

 

MP-16  The touch pad on the Milacron dryer wasn’t working. I called & requested a quote from Uni-Dyn.

 

MP-11  The core pull hydraulic hose came loose at the threads behind the quick-connect. It was never tightened. I cleaned up an oil pond around the press.It ran all night

     & nobody saw it leaking.

 

Dryer- D-7 on the mezzanine had a bad regin. contactor. Replaced

 

 

10/9/10

 

Mezzanine -  I played musical dryers all day to get one that worked.  I pulled D-6 off station 2  & took it to the shop. I replaced it with D-32 from floor. I looped out

      D-7 on station 4, to try & dry the beds. I also loop out D-6 in the shop to see if it would dry out. After several hours, D-7 came down to – 40, so I put it on station 2.

      D-32 wasn’t drying, so I looped it out.  D-32 & D-6 , after  6 to 8 hours, the dewpoint is finally starting to drop somewhat.

 

MP-3 Installed core plug on the steemer handle mold.

 

MP-1 Die height alarm- The position had to be moved manually before the auto die height function would work.It was too close to the end of the threads to lock in.

         After that, it was getting an eject alarm----- I found the knock-outs weren’t tied in. OK  now.

 

MP-3  Robot was alarming out – not seeing eject. forward.  Found the multi-eject. on the special option page was not turned on. OK now.

 

Friday, October 8, 2010

Ronnie Upchurch

MP-23  I worked with Mark M. setting up the new eoat for the 2 cav. fan  mold 74022.

 

MP- 6  The mold wouldn’t close. I checked all the limit switches & found the operator side gate switch wasn’t making. I adjusted the jam-

      bar  flag.

 

MP- 1  It was getting a lube alarm. Josh reset the manual lube count to the maximum setting.

 

Two molds fell off the pallet while being transported.  We got them stood up & checked them out for damage. Mold 76003 cav.1 had a broke strap bolt.

       76003 cav. 2 had a pinched wire & cracked mounting brackets on the heater junction box. All is repaired except the box. We can fix it when they

       Finish the run on MP-6.

 

MP-17 Cleaned up oil .

 

MP- 6  Vacuumed out oil pan. Oil vac. is still behind the press.

Wednesday, October 6, 2010

10.5.10 Sean D-shift

Mp#5- Put the EOAT w/gate cutter back on and set values into the controller from the set-up sheet. Should be ready to start up.

Re-did some hydraulic core 2 fittings that were leaking and had been red tagged for repair. No further leaking.

Mp#3- Put the new EOAT w/gate cutter on and set it in as close as possible w/out running parts. I dry cycled it several times to check operation and get it timed close. May need to adjust the clamp position and ejectors, or the Y-axis up or down.

CAUTION!- The cutters are very SHARP. I bumped into them and punctured by hand!

Set the dryer temp correctly on the stainless cincinatti dryer on the mezzanine. It went down for wet material mid-shift, and after looking at it, it had been set to 32 F..?
Set it at 180 and it has been running fine.

Call if you have any questions. Be back Friday.

Josh-I submitted the rest of my PTO for the year, on your desk.

Thanks,

Sean

Friday, October 1, 2010

9.30.10 Sean

Mp#2- Smashed core wires twice. They have been tied up as neatly as possible to prevent further problems.

Got called into the assembly area to assist with helping the girl get the programming software working for the stepper drivers in the lab. ?

Mp#1- baseplate press stopped operating. Found sensor loose on the shuttle forward position.

Mp#21- while doing the PM I found the press had no control power. Looking further, it seems that the power from the disconnect on the bus was 100 volts short on the brown leg?
Mark and Gary are investigating that further now.

Have a portable hopper loader receptacle that is broken, may need to either order a replacement receptacle or rewire with something else on both ends.

Worked on PM's the rest of the time in between activities.

Call if there are any questions. have a great weekend.

Sean

Thursday, September 30, 2010

9.29.10 Sean

Mp#5- They had a problem with the cores not working at all.
I went through replacing hoses and checking with the test cylinder and still was not working. Put gages on and had pressure at valve, but not at cylinders.
They would work when i probed valve m,anually.
Then I checked voltages at coils and had none on the set side.
At this point neither core 1 or core 2 were working but I was focusing on #1 for now.
Then I noticed that the output menu 41 slot 6 would energize 2 outputs when trying core 1, but the card was only lighting up the led for pressure and not the set output.
I tried swapping the card and then both sets of cores started working.
I suspected that there was a problem with the output card that I had moved to slot 8 so I left it down until we could find another one.
Ronnie mentioned that they had worked on it today but was not real sure what was done to get it going again.
I would like to know what you found?

Also had the problem with the Chilled water supply being dirty, in which I discovered, after speaking with Ronnie colson, that there is no filtration on the Chilled water system.? I temporarily bypassed the pressure switches on the Thermolators pumping chilled water until the problem is resolved and we have taken the corrective actions.

Call if there are any questions. Enjoy your evening!

Sean.

Ronnie Upchurch

MP-15  Oil leak.  I am ordering a new pump seal for this one.

 

We were having problems with thermolators cutting off on MP-2 & 3. ( chiller supply )  The flow & temp looked OK.  In tooling the EDM was over heating.

     they bled the line & got quite a bit of air & rusty water out. After that, the thermolators straightened out. There must have been an air lock.

     Ronnie Coleson was notified.

 

I installed the new overload on MP-5. They will hang the base plate back in.

 

If the hydraulic oil doesn’t come in today, I’ll call them in the morning.   

Wednesday, September 29, 2010

Mike Daniels-B Shift

Good morning Gents,

 

Typical night in molding no major problems. Mp2 has a issue with the core switches, the i/o page shows they are set when they are and pulled when they are but when put in cycle clamp moves about 6in. then stops and reads core 1 not pulled when it is. We ran it on timers  with no problems.

Repaired 3 more trollies

Replaced prox switch on fixture on mp10

Replaced blown nozzle heat fuse on mp2

 

Have a great day

Gone Fishin

 Mike

Tuesday, September 28, 2010

Sept 28, 2010

MP5 keeps tripping overload on pump.  A complete contactor and overload should be here Wed. UPS Red.

They moved the baseplate mold to #1.

 

Lexan sheets came in today.  Been trying to replace broken panels in trolleys as I can, if you pick up where I left off, measure each one individually as there are slight differences between them.

 

 

Mark McKee

Technical Specialist

Oreck Manufacturing Company

1400 Salem Rd

CookevilleTN  38506

mmckee@oreck.com

PH      931.646.7856

CELL  931.644.5289

FAX    931.646.7615

 

Monday, September 27, 2010

9.26.10 D-shift Weekend

Stripped equipment Friday. Reassembled the grinder on Saturday.
Worked on PM's Sunday. Turned in some work orders for some of the issues we had.
There was a problem with #4 that had to do with frayed core wire and a blown fuse.
We cleaned out all the water strainers on all the presses this morning.
I have noticed that the moisture in the air system seems to have been resolved.

I will be coming in on Wednesday at 10a.m. for Forklift refresher training. Afterwards I will see whats going on with our PM program. call if there are any questions.

Have a great day!

Sean

Sunday, September 26, 2010

Ronnie Upchurch

One of the bucket tumblers quit working. I just had to tighten the belt. I asked Elaine to order two more motors for the two spare tumblers. I put them

       in the trailer for now.

 

MP-7  The bolts vibrated loose & the deflector fell in the grinder. I cleaned it out & restarted it. It still needs a new deflector.

 

MP-2  I hooked up the cores to the eject circuit for them. Also replaced a broken core switch on the stationary side. One of the mold heater plug pins was pushed in

        & not making contact; repaired.

 

MP-6  The clamp wouldn’t close. I tried probing the valve, no luck. When I opened the cabinet to check the input & restarted the pump, it started working.

 

I worked on stripping & scrapping equipment in shop. I cleaned out the cabinet in the bone yard.

 

I finished up on the grinder that Sean put back together. We put it back in service Sunday.

 

Cleaned up oil on 17 & 21.

 

I put the gaylord of spare parts in the trailer.

 

Tuesday, September 21, 2010

Ronnie Upchurch

MP-2  Nozzle heaters quit working. Found blown fuse & shorted wire on front band. The blown fuse was 20amp -  should be 15amp -  Replaced

          with correct fuse.

 

MP-15  The chuck was closing before it reached the sprue. Changing the timer or mode didn’t work. I found that when I removed the air exhaust

       muffler, It worked fine. I tried to clean it & reinstall it, but didn’t work, so I left it off.

 

MP-4  We still have a leak at the top of the eject. pump. It looks to be coming from the bottom of the block where the boss fitting ties in. If they  don’t

       shut it down in the next two days, I’ll get it when I get back Friday.

 

I’ve been bleeding a lot of water out of the air lines today; loaders, robots, & support equip.

 

I started vacuuming oil pans – MP-4 -6 & 7.

 

The chiller temp. started climbing again. 70 degrees in the shop. The temp. was set at 48, but actual was 57. I called Ronnie C. & he said he would

      come out & start the other chiller.

Ronnie Upchurch

I worked with Mark some in MRO, sorting parts that were stored in gaylords.

 

Mezzanine – DR-1 had two bad regin. heaters. Replaced.

 

Mezzanine -  DR-32  The turntable got in a bind because the limit switch was adjusted too tight against it. One of the motor gears stripped out &

              two teeth on the bed gear broke off. I replaced the motor. We had to order another bed gear. I swapped the dryer out on the mezzanine.

 

Mark replaced the nozzle heater on MP-13.

 

MP-17  Oil on the floor & the jug was full “ Again .“  Cleaned up.

 

New  hydraulic fluid has been ordered.

9.20.10 D-Shift

Matsui dryer not heating up to process temp.

The control does not appear to be outputting any contactor signal.

I am going to look at it again this evening to try and be sure that everything other than the controller is working alright. I suspect that there could be an input such as a switch or sensor causing the control not to output.?


I organized the machine and equipment manuals and labelled everything as well as possible. Maybe we can keep it this way?


Next problem is Brelands' encroaching desk area!


I could have made some mistakes in identifying presses with particular manuals so if anyone finds something wrong let me know or pencil it in and we can have some form to our function! I followed the asset list by serial number and old press number before labelling them. They are separated by machine brand, (i.e. Nissei, Milacron, and Toshiba, etc.)


Call if you have any questions, have a great day!
Sean





Sunday, September 19, 2010

Mike Daniels-B Shift

Good morning,

Just a few issues last night

Replaced 4 nozzle bands on mp20 due to bleed off. Apparently it ripped wires from bands when sled was backed off.

Replace lexan in 2 buggys from junk yard and placed them in molding

Replaced a e-stop switch on grinder at mp6.ginder wouldn’t run

A core wire on mp2 got cut and shorted out blowing a fuse.

Swept the shop.

 

Have a Great Day

Mike

Saturday, September 18, 2010

Mike Daniels-B Shift

Good morning all,

 

Quiet night no major problems on molding floor. I put the new control in matsui drier, its still in shop I let it run for around an hr or so with no problems so I green tagged it.

 

Have a great day

Mike

 

Friday, September 17, 2010

9.16.10 D shift continued.

Also, thought you might like to know that Marty informed me that he and Darryl might be trading shifts per Wayne's decision.??

9.16.10 D shift

Mp#8 - Mixer was leaking material from cylinder not shutting off flow from hopper.
Lubricated the cylinder and had no other problems with it.
May have to replace the cylinder (one on the back side) if there are any other problems.

Repaired one of the small conveyors.

Stripped major components from that dryer and put the rest of it in the scrap metal hopper.

Put one of the slow speed grinders back into circulation.

Added a task to the task list for the DME boxes, per Mark.

Cleaned up in the shop, took out trash and cardboard, swept, and picked up behind the metal shear in the shop.

Call if there are any questions.

Sean

Thursday, September 16, 2010

Ronnie Upchurch

 MP-16   Dryer  D-9 Temp. probe alarm.  They were running it at 250 & the High limit was at 200. Reset- OK.

 

Loader #6 on mezzanine not loading. The loader flap was stuck & not making the switch.

 

MP- Lube cycle alarm. Reset the counter & installed a new tube of grease.

 

MP-The boss fitting on the top inj. pump line was leaking. I took the line & fitting off ; the o-ring was cut. Mark had to go to IR-G to get

       the right o-ring. He reinstalled it – looks good.

 

MP-9  The  C- axis on the robot wasn’t working. I found a cracked air fitting at the solenoid. Also the coil piston was gummed up.Cleaned &

          reinstalled – Working good.

9.15.10 D shift

Mp#10-Robot- Stopping infrequently over the belt after part delivery.
Restarts fine, then runs for a few hours until it does it again. Has not stopped in awhile, they want to keep running it.

Moved everything out of the trailer out back and staged it to the left of the dock per Josh. Should be easy to sort and move now.

Put all of the items tagged for "shop" or to "strip" in the shop. Also Ronnie and I put the grinder from the bunker back in the shop and put the little one that was in the shop to the bunker.

Removed all of the Yushin pickers from the machines and located them in the staging area as well.

Mp#6- replaced nozzle heater band and repaired wiring from blow back.

Cleaned up the oil from #17 again.

Cleared the lubrication alarm on MP#1 also.

Swept up in the shop.

Call if there are any questions!

Sean

Tuesday, September 14, 2010

Mike Daniels-B Shift

Good morning,

 

Fairly peaceful night, minor adjustment on nippers on the fixture on press 3.

Tried to calibrate gravity loader on the dryer that is behind press 8 it still not acting right

Removed another small nozzle leak from press 15 no damage only down couple minutes.

 

Have good day

Mike

Monday, September 13, 2010

9.13.10 D shift weekend

Worked on Pm's for machines.
Started putting the core 2 stuff on 23.
Helped with processing some this weekend, we were short 1 tech.
Worked on the nut press cleaning the phosphate build up out of the tracks.

We need to order some repair parts to get some of our DME boxes back up and going again. a few have collected in the shop as well as some cards.
It would be nice if the techs could tag them with a brief description of what has been wrong with each card?

The weekend went relatively well.

Call if there are any questions. Have a great day.

Sean

Thursday, September 9, 2010

Josh A Shift 09/09/2010

Hello All,

They finally released some funds to order parts to repair one of the two grinders we still have tore down.  I chose the bigger one and ordered the parts for it today.  I’ll order the parts to repair the little Solo grinder next month.

Also, I’m got approval to do a CER tomorrow for two New Grinders specified for Pelethane (Santoprene).  I chose to go with AEC because they have recently purchased Cumberland and Nelmor which are both good brands.  I sent them a box of our runners to heat up and do grinding trials on.  Rapid makes a good grinder, but I just guess the cheap ones Hank bought have left a bad taste in my mouth.

Attached are the specs and quote so that everyone can check it out.

 

Thanks

 

  Joshua Ledbetter

  Molding Maintenance Manager

  Manufacturing Engineer

  Oreck Manufacturing Company

  931-239-3235

 

Mike Daniels-B Shift

Good morning, 

                       

 I helped Gary replace dump cylinder on pump#1 on mezz. It was sticking at start of shift. Went ahead and replaced the cylinders on pumps #2,3,4 and 5(per josh) found that the flange on pump 3 was cracked bad. I called Josh to see if we had a replacement,(we didn’t) so I tig welded it back together and Josh and I put it back together. Probably down 2hrs. Other than that fairly peaceful night in molding.

 

Have a great day.

Tuesday, September 7, 2010

Ronnie Upchurch

MP-20  Nozzle adapter heater band was bad---- replaced.

 

MP-25  The cores were backwards.  Normally the core cylinder is fixed & the shaft moves ;  on the hokey handle mold the cylinder moves , so the

            set & pull lines hook up backwards.

 

MP-25  Replaced the motor overload on the grinder.

 

MP-2  The rear zone heater - mercury contactor blew up. Mark & I  contacted Walter Marcum. We cleaned out the cabinet & disposed of the mercury

          In the drum in the recycle room. Installed a new contactor.

  

Friday, September 3, 2010

9.2.10 D shift

Mp#2 Grinder- It was overfilled with material and clogged up almost to the point of meltdown. We unclogged it and cleaned it out reset the breaker and tightened up the E-stop switch. Put back in use.

This occurred at 6:05 pm and had to have been clogged for at least a half an hour earlier on C shift, before our shift began.

This would make a good action item for September!

Vibratory Welder- Did a full P.M. on it. Tightened up door limit switches, brackets, and checked out hydraulic unit. greased the linear rails and inspected for anything loose. Relabelled tubing and Mark and I reset the adjustments on the laser range sensors.

Repaired leaking core fittings on the single cavity top cover tool in #11.

Continued with PM program, lubed tie bars and refilled reservoirs, checked for damged lines etc.

Have a good weekend.

Sean

Thursday, September 2, 2010

9.01.10 D shift

Mp#4- Built EOAT for Edge Baseplate. Got it running, had to adjust Core pressures and flow controls. Was operating below 5oopsi. Now around 1600psi.

Mp#15- did PM on sprue picker. Repaired stripped out screw on advance stroke adjustment plate. Greased and inspected.

Repaired broken lube line on non-op side platen skate. replaced the nylon tubing with a piece of aluminum tubing. Hopefully it will last longer this time.

Chaged out EOAT on #11 for the Edge Top-cover core.

Set-up robot on press #23 for top cover single cavity tool.

Mostly helped process techs tonight, as we had one leave early in the shift for personal issues so we were short handed.

Will continue P.M. program tonight. Need to look into a way of tracking which ones are getting done so that we do not miss any.

Call if there are any questions.

Sean

Monday, August 30, 2010

August 30, 2010

Upgraded robot displays with speed control adjust on MP3, 8, 9, 10, and 11 today.

 

Ran chiller water to the dryer behind MP8 off the machine manifold and hung a sign on the ball valves, not to shut off unless machine pump and dryer are shutdown first.

 

Mark McKee

Technical Specialist

Oreck Manufacturing Company

1400 Salem Rd

CookevilleTN  38506

mmckee@oreck.com

PH      931.646.7856

CELL  931.644.5289

FAX    931.646.7615

 

Test for Mike Daniels

Test

8.29.10 D-shift

Mp#5- Stopped once at 6:30pm, the back door had come ajar. Locked it closed. No further problems with it. Ran all night fine.

Mp#1-
Removed all of the panels from the press and thoroughly cleaned them and inspected all of the lubrication joints. Many were hand loose. Went over all of them with a wrench. All of the lines are in satisfactory working condition. The ones on top of the moving platen have obviously been stepped on a few times but are secure and intact.


Inspected the servo drive belts and mounting brackets on all of the drives including the clamp. They had no cracks or signs of needing replacement yet, other than the extruder belt which I noticed had some damage when I put the barrel back together. It is running very close to the flange on the drive pulley. The problem is that there is not any obvious way to attempt to adjust the "Tracking" or "center" the belt. It only has a tensioning screw. Shimming it might cause it to run back but then there would be the risk of it running back againt the servo motor.
Because of that, I made no adjustment to it without getting more feedback first, it may have came in like that?
.

I went through the list of items this weekend and had some questions as to where the Asset tags needed to go and which presses to put them on so if you can refresh me on that I will try to get those mounted Wednesday when I return.

the Hot stamp press that Ronnie worked on stayed on all night so it should be ready to use again. The heats did not go off.

Also wanted to get more input on the EOAT bench needed for the EOAT area before fabricating. There is a cart there now, did you want to make it portable? Should I check with Wayne? Was that his idea? ...Just Kidding.

Call if you have any questions.

Sean

Sunday, August 29, 2010

" C " Shift - Weekend

MP-20  The cycle start timer wasn’t working. We saw input 14 on the plc flickering. Mark traced the wire & found a loose connection in the robot wiring.

 

MP-5 Added hydraulic fluid.

 

MP-2 & 6   PMed.

 

MP-20  Mold # 77015 – The DME heater plug on the mold had a broke pin – zone 6. I replaced the plug. The wires were short in the box so I had to add another splice in       the wiring.  I’ll have tooling let me

               know  when  the mold comes back & I’ll fix it right.

 

MP-5  Pump motor overload tripped. Injection valve – off  fault.  Mark said the pack time was  set too high.  He lowered the time & it hasn’t stopped again.

 

MP-3  Zone 3 barrel temp was running away. The mercury contact was stuck- replaced it.

 

I worked on the bag clip hot stamp. The heat kept dropping out. I found a loose solder connection on the board. I re- soldered it & I have been trying it out

      In the shop. So far I hasn’t cut off.

 

 

 

   R. Upchurch